* patch "iio: magnetometer: ak8974: Fix runtime PM imbalance on error" added to staging-linus
@ 2020-07-08 7:21 gregkh
0 siblings, 0 replies; only message in thread
From: gregkh @ 2020-07-08 7:21 UTC (permalink / raw)
To: dinghao.liu, Jonathan.Cameron, Stable, linus.walleij
This is a note to let you know that I've just added the patch titled
iio: magnetometer: ak8974: Fix runtime PM imbalance on error
to my staging git tree which can be found at
git://git.kernel.org/pub/scm/linux/kernel/git/gregkh/staging.git
in the staging-linus branch.
The patch will show up in the next release of the linux-next tree
(usually sometime within the next 24 hours during the week.)
The patch will hopefully also be merged in Linus's tree for the
next -rc kernel release.
If you have any questions about this process, please let me know.
From 0187294d227dfc42889e1da8f8ce1e44fc25f147 Mon Sep 17 00:00:00 2001
From: Dinghao Liu <dinghao.liu@zju.edu.cn>
Date: Tue, 26 May 2020 18:47:17 +0800
Subject: iio: magnetometer: ak8974: Fix runtime PM imbalance on error
When devm_regmap_init_i2c() returns an error code, a pairing
runtime PM usage counter decrement is needed to keep the
counter balanced. For error paths after ak8974_set_power(),
ak8974_detect() and ak8974_reset(), things are the same.
However, When iio_triggered_buffer_setup() returns an error
code, there will be two PM usgae counter decrements.
Signed-off-by: Dinghao Liu <dinghao.liu@zju.edu.cn>
Fixes: 7c94a8b2ee8c ("iio: magn: add a driver for AK8974")
Reviewed-by: Linus Walleij <linus.walleij@linaro.org>
Cc: <Stable@vger.kernel.org>
Signed-off-by: Jonathan Cameron <Jonathan.Cameron@huawei.com>
---
drivers/iio/magnetometer/ak8974.c | 19 ++++++++++---------
1 file changed, 10 insertions(+), 9 deletions(-)
diff --git a/drivers/iio/magnetometer/ak8974.c b/drivers/iio/magnetometer/ak8974.c
index 810fdfd37c88..041c9007bfbe 100644
--- a/drivers/iio/magnetometer/ak8974.c
+++ b/drivers/iio/magnetometer/ak8974.c
@@ -862,19 +862,21 @@ static int ak8974_probe(struct i2c_client *i2c,
ak8974->map = devm_regmap_init_i2c(i2c, &ak8974_regmap_config);
if (IS_ERR(ak8974->map)) {
dev_err(&i2c->dev, "failed to allocate register map\n");
+ pm_runtime_put_noidle(&i2c->dev);
+ pm_runtime_disable(&i2c->dev);
return PTR_ERR(ak8974->map);
}
ret = ak8974_set_power(ak8974, AK8974_PWR_ON);
if (ret) {
dev_err(&i2c->dev, "could not power on\n");
- goto power_off;
+ goto disable_pm;
}
ret = ak8974_detect(ak8974);
if (ret) {
dev_err(&i2c->dev, "neither AK8974 nor AMI30x found\n");
- goto power_off;
+ goto disable_pm;
}
ret = ak8974_selftest(ak8974);
@@ -884,14 +886,9 @@ static int ak8974_probe(struct i2c_client *i2c,
ret = ak8974_reset(ak8974);
if (ret) {
dev_err(&i2c->dev, "AK8974 reset failed\n");
- goto power_off;
+ goto disable_pm;
}
- pm_runtime_set_autosuspend_delay(&i2c->dev,
- AK8974_AUTOSUSPEND_DELAY);
- pm_runtime_use_autosuspend(&i2c->dev);
- pm_runtime_put(&i2c->dev);
-
indio_dev->dev.parent = &i2c->dev;
switch (ak8974->variant) {
case AK8974_WHOAMI_VALUE_AMI306:
@@ -957,6 +954,11 @@ static int ak8974_probe(struct i2c_client *i2c,
goto cleanup_buffer;
}
+ pm_runtime_set_autosuspend_delay(&i2c->dev,
+ AK8974_AUTOSUSPEND_DELAY);
+ pm_runtime_use_autosuspend(&i2c->dev);
+ pm_runtime_put(&i2c->dev);
+
return 0;
cleanup_buffer:
@@ -965,7 +967,6 @@ static int ak8974_probe(struct i2c_client *i2c,
pm_runtime_put_noidle(&i2c->dev);
pm_runtime_disable(&i2c->dev);
ak8974_set_power(ak8974, AK8974_PWR_OFF);
-power_off:
regulator_bulk_disable(ARRAY_SIZE(ak8974->regs), ak8974->regs);
return ret;
--
2.27.0
^ permalink raw reply related [flat|nested] only message in thread
only message in thread, other threads:[~2020-07-08 7:21 UTC | newest]
Thread overview: (only message) (download: mbox.gz follow: Atom feed
-- links below jump to the message on this page --
2020-07-08 7:21 patch "iio: magnetometer: ak8974: Fix runtime PM imbalance on error" added to staging-linus gregkh
This is a public inbox, see mirroring instructions
for how to clone and mirror all data and code used for this inbox;
as well as URLs for NNTP newsgroup(s).